siemens/mc_apl1: Correct the Tx signal from SATA interface

Because of an incorrect transmit voltage swing, the signal must be
adjusted. The factor of slices for full swing level can be corrected via
the High Speed I/O Transmit Control Register 3.

Change-Id: I116802cd2a944658fc3022e948eba43cebe52bb4
Signed-off-by: Mario Scheithauer <mario.scheithauer@siemens.com>
Reviewed-on: https://review.coreboot.org/28285
Tested-by: build bot (Jenkins) <no-reply@coreboot.org>
Reviewed-by: Werner Zeh <werner.zeh@siemens.com>
Reviewed-by: Alex Thiessen <alex.thiessen.de+coreboot@gmail.com>
This commit is contained in:
Mario Scheithauer 2018-08-23 15:33:53 +02:00 committed by Werner Zeh
parent aef592d9b6
commit e27c096b7f
2 changed files with 11 additions and 0 deletions

View File

@ -27,6 +27,8 @@
#include <baseboard/variants.h>
#include <variant/ptn3460.h>
#define TX_DWORD3 0xa8c
void variant_mainboard_final(void)
{
int status;
@ -63,6 +65,14 @@ void variant_mainboard_final(void)
* offset 0x341C bit [3:0].
*/
pcr_or32(PID_LPC, PCR_LPC_PRC, (PCR_LPC_CCE_EN | PCR_LPC_PCE_EN));
/*
* Correct the SATA transmit signal via the High Speed I/O Transmit
* Control Register 3.
* Bit [23:16] set the output voltage swing for TX line.
* The value 0x4a sets the swing level to 0.58 V.
*/
pcr_rmw32(PID_MODPHY, TX_DWORD3, (0x00 << 16), (0x4a << 16));
}
static void wait_for_legacy_dev(void *unused)

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@ -33,6 +33,7 @@
#define PID_ITSS 0xD0
#define PID_RTC 0xD1
#define PID_LPC 0xD2
#define PID_MODPHY 0xA5
#define PID_AUNIT 0x4d
#define PID_BUNIT 0x4c